Collisions - 1995
 

Date: 21-APR-95 Operator: Texaco, Inc.
Investigation: Complete Activity: Development
Lease: G02241 Event(s): Collision / Pollution (11.9 bbls)
Area: West Cameron Operation: Production / Motor Vessel
Block: 643 Cause: Weather
Rig/Platform: A Water Depth: 375'

Remarks: A standby boat was offloading a snubbing unit when rough seas and high winds pushed the boat into the platform. This resulted in a ruptured diesel tank.
 

Date: 28-JUN-95 Operator: CNG Producing Company
Investigation: Complete Activity: Development
Lease: G03969 Event(s): Collision / Pollution
Area: West Cameron Operation: Production
Block: 478 Cause: Vessel Struck Platform
Rig/Platform: A (removed) Water Depth: 123'

Remarks: A ship or barge struck the southeast corner leg of the platform, which may have caused a small underwater leak in the departing pipeline. The aids to navigation were working before and after the accident. A derrick or lay barge may have caused the damage. On June 29, 1995, CNG reported that the pipeline was not leaking and was holding 1000 psi.
 

Date: 11-JUL-95 Operator: Phillips Petroleum Company
Investigation: None Activity: Development
Lease: G02412 Event(s): Collision
Area: High Island Operation: Other / Preloading Rig
Block: A317 Cause: Equipment Failure
Rig/Platform: A Water Depth: 217'

Remarks: A rig was positioned on the NE corner of the platform. The bow leg had been preloaded and preload had been dumped. The port leg had been preloaded to about 50% when the leg penetrated about 8 feet into the soil causing the rig to lean into the platform. There was structural damage to the platform. No spills or injuries occurred.
 

Date: 21-JUL-95 Operator: Hall-Houston Oil Company
Investigation: Complete Activity: Development
Lease: G05322 Event(s): Collision
Area: West Cameron Operation: Other
Block: 421 Cause: Human Error
Rig/Platform: B Water Depth: 105'

Remarks: A work boat was tied up for the night at the platform, waiting on daylight to begin work. The workboat and the platform were struck by a tug pushing a 180' notch barge. No personnel were injured, and no pollution was observed. The flowline/pipeline and handrails were damaged and will need to be replaced.
 

Date: 01-SEP-95 Operator: Texaco Inc
Investigation: Complete Activity: Development
Lease: 00310 Event(s): Collision
Area: South Marsh Island Operation: Production
Block: 229 Cause: Human Error
Rig/Platform: 106 Water Depth: 20'

Remarks: The remote monitoring and control operator located at the platform found that the RTU signal was no longer being received. Personnel were dispatched to the well and found the RTU antenna bent and the fog horn and navigation light toppled from their welded stand. Cable scrape marks were found on the hand rail adjacent to where the fog horn was located. There were no boats tied to the structure, although many shrimp boats were in the vicinity.
 

Date: 03-OCT-95 Operator: Meridian Oil Inc
Investigation: None Activity: Exploration
Lease: G14200 Event(s): Collision / Pollution (89.0 bbls)
Area: Matagorda Island Operation: Drilling / Motor Vessel
Block: A371 Cause: Human Error / Weather
Rig/Platform: Rowan Gorilla IV Water Depth: 430'

Remarks: A weather change caused the motor vessel to drift into the port leg of the drilling rig resulting in punctures to the saddle tank of the boat and the release of approximately 3,722 gallons of diesel fuel. Due to rough weather and sea conditions, no attempt was made by the boat company to recover the spilled fuel. There was no damage to the drilling rig, and the boat returned safely to shore.